OK, So I reinstalled the BB by tightening the NON-drive side first. I noticed the lockring appears to be almost flush with the cup & BB shell with hardly any threads extending past it. Test rode about 1 mile and everything is nice and snug. I assume that was key step, to tighten the non-drive side first, but I just can't seem to figure out why this is so. Oh well.
Hope to take it for a real ride later today which will be the real test. Thanks for all of your input. Hopefully the problem has been resolved.
Hope to take it for a real ride later today which will be the real test. Thanks for all of your input. Hopefully the problem has been resolved.